15 January 2010 Company Announcements Platform Australian Stock Exchange Limited Exchange Centre 20 Bond Street SYDNEY NSW 2000 Via ASX Online
SUGARLOAF OPERATIONS UPDATE
Adelphi Energy Limited (Adelphi) provides an update on operations within the Sugarloaf AMI. Kowalik #1H - Fracture Stimulation Program
Following the decision to tie back the liner at Kowalik #1H, having observed an anomalous pressure drop at the end of the main fracture stimulation stage, a rig was mobilized to the wellsite to carry out the necessary work. During one of the final stages of this work, when cement had been circulated into the annulus of the tie back string, a section of slim drill pipe being used as a running string for the tie back string parted some 700ft below surface. The initial fishing activities have so far recovered tubing down to a depth of 8,150ft but in light of the other activities commencing within the Sugarloaf AMI, it has been decided to suspend operations on Kowalik #1H so that further evaluation and planning can take place before reentering the well.
The workover rig is presently being demobilised from the location. This will lead to a further delay before Kowalik #1H can be prepared for flow testing following the fracture stimulation carried out on 28 December 2009.
Easley #1H Spud Date for new Horizontal Well
Adelphi has been advised by the Operator, Texas Crude Energy Inc (TCEI), that the Patterson #150 drilling rig commenced mobilization to the Easley #1H rig site on Thursday, 14 January 2010. It is expected that the well will be spudded early in the week beginning 18 January 2010. Easley #1H is the first new well to be drilled under the farmin agreement with Hilcorp Energy within the Sugarloaf AMI.
Kennedy #1H Scheduled Commencement of Fracture Stimulation Program
Adelphi has been advised by TCEI that the Kennedy #1H fracture stimulation is scheduled to commence on Monday, 18 January 2010. As previously advised, the 4,000ft of horizontal liner will be fracced in 14 separate stages with an isolation plug set between each stage. The operation is expected to take 7 10 days after which the isolating plugs will be drilled out and the well cleaned up and then flowed to sales.
easley is spudding in the next few days and kennedy is being fracced on monday
kowalik is very much a work in progress, the down hole issue this time is unrelated to the previous issue, the casing looks to be not as one would like it to be at all to say the least. the workover rig is off site while they engineer the next step. did they drill on an a cursed indian burial ground or something?
ADI Price at posting:
17.0¢ Sentiment: Buy Disclosure: Held